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The
trials and tribulations of owning a 1925 Indian Scout by
Bill Phelps
(Click
the photos to see them in full size then use the back button to return)
Someone
said that it would be nice to read about someone’s restoration efforts,
well
this story is not so much about a restoration but about commissioning a
bike
that should have been right from the start.
So,
first catch your bike. Easier said than done when looking for an
Indian. I
found a few on the continent and at one point did talk to a Dutch firm
who had
two for sale. A 1926 black one for a fairly high 14,000 euros and a
1927 red
one at 19,500 euros (ok, you work it out). I crossed the 1927 bike off
my list
as being just too expensive, although it did have all the ancillaries,
whilst
the black one had none, no lights, horn, speedo, etc. I became half
interested
in the black 1926 model, and decided to see if I could part ex my 1904
Givaudan.
Several emails later and after a derisory offer of 3000 euros had been
made for
the Givaudan, I crossed the 1926 bike off my list. After all, it was
black and
was no doubt the correct colour, but all Indians should be red,
shouldn’t they?
Plus the bike had wired on tyres and a front brake, both changes that
didn’t
come in until 1928 – I’d been doing my homework, you see.
A
friend in Belgium,
called
Ronnie Bracke put me on to a small dealer in The Hague who
had a 1925 Scout for sale. The
bike looked good from the photos and I had a pile more emailed to me,
plus the
engine number – Indians didn’t number their frames until 1931.
Everything
looked to be right and it had a dynamo fitted as well as a rear light.
No
headlamp or switchbox. So, the bike was put on my short list. Meanwhile
I was
put onto a 1930 Scout which was about to come on to the market in the
UK.
It was the
actual machine that Titch Allen had road tested in his sixth Vintage
Road Test
Journal. Things looked promising but in the end the seller’s wife told
him that
he ought to keep it as he wouldn’t get another anywhere near as good.
So, now I
was left with only the 1925 Scout in The Hague, but
what a way to go just to have a look.
During August 2007
we planned to ride in the Oude Klepper Parade in Belgium with the 1908
Triumph and then we
intended to move on to Hengelo
in Holland
for an event on
the following weekend. It seemed an ideal opportunity to run the 75
miles to The
Hague and have a look
at the bike.
We
did that and easily found the small shop in Delft where the
guy promptly wheeled the bike
out into his back yard. I spent some time having a good look and all
seemed
fine. “Is there a headlamp?” I asked. “No, sorry“ came the reply.
Making a
mental note that I’d needed a headlamp and switchbox, plus a horn and a
complete
speedo and assembly, we set about starting the bike. The motor was soon
running
and I listened for any rattles and clanks – all sounded good as he
blipped the
throttle. There was some oil leakage here and there, which I just
ticked off as
a couple of small jobs to be done when I got the bike home. I offered
what I
thought was a fair price and after checking the exchange rate the guy
agreed
and we shook hands – I had my bike, well, nearly. The transfer of the
money
took some sorting out and Josie came to the rescue as she was used to
it. I
agreed that after the money was with the dealer the following day that
we would
collect the bike on the way home after the following weekend at Hengelo.
I
had on my trailer my 1908 Triumph and sidecar and my 1936 Nimbus so had
to make
room for the Indian. The sidecar was removed from the Triumph and it
was
completely dismantled and ‘flat-packed’ in the back of the car with
Terry
taking the basket in his camper, whoops, sorry, motor-home.
On
the way to The Hague
to collect the Indian the
engine of my car decide to let go in a big way when out in the third
lane on
the motorway around Arnhem,
but all that’s another story. We dumped the car, caught a flight back
to
Cardiff from Schipol, near Amsterdam and the following day, after
borrowing our
sons Volvo estate, we were back in Arnhem to collect the trailer and
all our
belongings –plus, of course, the Indian.
The bike was loaded up and the
dealer
invited us back into his shop for a coffee, before we set off. Would
you
believe it, there on the floor were as set of boxes and laid out on top
of them
was a headlamp, switchbox and complete speedo set-up – just what I
wanted. I
asked if they were for sale and was told – “not really, I bought them
for my
wall-of-death bike”. He then said that he could perhaps let them go and
started talking of £1600,
Jean shook her
head, so I apologised and said that I’d get back to him. On the way
home I
asked myself the question – who the hell would put lights, horn and a
speedo on
a wall-of-death bike, after all, I’d ridden one on the wall in Brighton
back in the 1960’s. At
least my girl could see
that I was being tucked up.
Anyway,
it was great to get home and push all the bikes into the garage – all I
had to
do now was a bit of fiddling and register the bike. Hmmm, that’s what I
thought.
First
thing was to inflate the tyres a bit harder than they were. Beaded edge
tyres
need a much higher pressure than the modern wired on types – ask me if
you want
to know why. Pump up the tyres – how? I found that the inner tubes had
pedal
cycle valves. First thing to do then was to get a
‘proper’ set
of motorcycle inner tubes - they were ordered and delivered – out came
the wheels
and in went the new tubes. I could at least pump the tyres up without
resorting to
a bicycle pump. However, all was not that easy, read on.
To
remove the rear wheel I had to undo the brake
anchor,
like you do. It consisted of a plated metal strap around a frame tube
and was I
glad that I decided to do this job. The brake anchor strap was cracked
where it
had become too thin by the plater polishing the pitting out of it. Gee,
if I’d
have ridden the bike like that and put the brake on!!! The mind
boggles. After
making a new anchor strap and re-fitting the brake rod the correct way
round, I
turned my attention to the front end. For some reason or other it
didn’t look
right and the problem soon became obvious, the suspension was stuck in
the down
position and wouldn’t rebound back up. I found that the front pivot
bolt on the
end of the spring was seized solid in the eye of the spring. To get it
out I
had to resort to using my eight ton press to get some movement. That
sorted,
and new tube installed I thought that I’d grease the front suspension
bushes –
could I? - like hell. A close inspection and I found that when the
rocker arms
were plated the grease nipples were left in and they were plated over
as well.
New nipples fitted and after re-assembly I had a suspension that was
greased
properly and worked - oh, and I was able to pump the tyres up.
Checking
further around the bike, I found that one of the rear chain adjusters
was
missing and it was an oddball thread of ¼ x 24, which meant screw
cutting one
in the lathe. Another job done. Next I found that one of the bolts in
the top
of the gearbox, the very one used to bolt up the chainguard, had as
stripped
thread in the box itself. I managed to tap the hole out a slightly
larger size
and fitted a nice new stainless polished bolt. Now I turned my
attention to the
exhaust system as it sure didn’t seem to fit properly and the flange
nuts kept
slipping on their threads. That was an easy one, gently squeeze the
nuts on
each hexagon in the vice and the nuts then would lock up nicely. The
exhaust
itself did take some tweaking to get it to fit properly and after that
job I
was feeling quite pleased with myself. Continuing the inspection I
fitted a
split pin to the mag advance cable as well as two split pins to the
rear wheel
nuts. Next thing was to re-solder the cone back onto the oil pipe that
comes
from the tank hand pump as it was seeping oil. Another little job done
– hooray, soon be
finished, so I thought. Mind you I did find that the hand oil pump was
fitted with just a plain leather washer and that it wouldn't suck or
pump oil - all a case of someone not understanding that the washer
needs to be two, not one, and that they also need to be cup washers.
These things are easy to make out of leather and by the following day I
had them fitted in the pump so that it would do its job properly.
I
removed the battery for charging as it wasn’t
needed just yet due to there being no headlamp or
switchbox. I also removed the stop light
switch that
had been fitted – Indians didn’t have those in 1925. Next job – strip,
clean
and readjust the clutch as there was slip when trying to kick the bike
over.
So, to cheer myself up - let’s hear her run!!
Problem,
I couldn’t flood the carb – ‘what’s wrong with that’ I thought. Off it
came and
after having a good look I found that the float chamber body was on the
wrong
way round and that when I held it up to the light the float chamber was
not
locked up against the carb body – I could see daylight between the body
and the
float chamber. At this time I also had to make a new locking nut for
the top of
the butterfly to lock the operating arm up tight. There was also a need
to
adjust the air valve to get it to seat properly – don’t ask – there
isn’t
enough room here to talk about the intricacies of a Schebler carb.
Suffice to say that I even had to make a new float needle to replace
the well-worn one so as to get the float to shut off the fuel in the
horizontal position. So,
start
the bike I did and it sounded nice, must say – but!!! Oil leaked out of
the
head gaskets and out of two cracks in each of the two cylinders.
Off
came the heads and I found that all six head bolt holes in each
cylinder had
been helicoiled. Bloody hell, why? Ok, let’s see what we can do. I
tried
various things, PTFE tape on the bolts, then JB weld, to try and seal
the
cracks in the cylinders. All to no avail as when the heads were
tightened down
the bolts tried to pull the helicoils out of the cylinders and – hey
presto –
the cracks opened up.
Bob J very kindly took the
cylinders and welded
them up
for me. After a lot of fettling of the bores I refitted them and with
fingers
crossed started the motor, whereupon the cracks just opened up again.
Nothing
for it but to get the job done properly and the cylinders were sent off
for a
proper repair. Basically the cylinders had the cracks all ground out
into a vee
and were then put into an oven to get them cherry red so that they
could be
built up with good cast iron rods. Not an easy job and certainly not a
cheap
one.
When I got the cylinders back I
had the job of re-facing the tops
and
machining the bores to remove the excess weld. The photo
shows the cylinder mounted
on a spigot in the lathe and ready for the bore to be
machined. You can
see the welding inside the bore whilst the head face has been machined.Then drill and tap the
two
offending bolt holes in each cylinder. Looking at the job I was busy
cursing
the prat who had put all the helicoils in and, in a fit of annoyance,
decided that they all had
to go.
It
was a mistake to remove all the helicoils and I didn’t
realise until after I’d ripped them all
out that I would
need to make over sized studs and that instead of 3/8 x
24, I was
left with 7/16 x 24 threaded holes – and there’s no such thing as a
7/16 x 24
thread die to make the studs. What I did was to make a set of
shouldered studs
and screw cut the 7/16 x 24 threads in the lathe and then the other
ends 3/8 x
24 to take nuts – all to replace the bolts, which were incorrect
anyway.
Next
job was to machine the excess weld from the head face and the bores. I
managed
to do that – very carefully – ask me if you really want to know how I
did it. Final job was to get the cylinders re-nickled and I took them
up to
South Wales
Metal Finishers in Treorchy. What a smashing firm. “Give me a ring an
two days
and they should be done” I was told, so, two days later I rang and was
told
“yes” come and get them. What a refreshing change, to have a firm
actually do
what they said they’d do and not fob me off with an excuse.
I had to
run a
glaze buster down the bores to clean out the nickel as they had to
plate the
whole things. Blow me down; they’d done the job properly as the glaze
buster
took most of the nickel out and then the copper plate. The ‘proper’ way
of
plating an item is copper first, then nickel and finally chrome, if
that’s the
finish wanted.
Back
to the bike and all was assembled and the motor fired up – what ho, no
cylinder
wall leaks. I was so chuffed that every time some one visited I had to
demonstrate the bike – until Stewart’s turn came round – “listen to
this engine
then mate” I said as I kicked the motor over.
Down went my foot, just a
bit too
quickly as the kick-start snapped off, lousy welding, for sure. So,
I had another
job, repair the kick-start and make a proper job of it.
While
the cylinder saga was ongoing I turned my attention to the lights –
everything
that I needed could be bought in Holland,
but by this time I had an aversion to giving the Dutch any more of my
money. A
good Belgian pal of mine said to me once “If a Dutchman hasn’t cheated
you, then
it’s only
because he’s forgotten to”. I needed a headlamp and sourced a period
lamp from
John Ellis.
The brackets
were easily made and I then turned my
attention to the
switchbox. It sits on the top tube and has an ammeter set into it with
a light
switch on the rear end. From Holland
they are 325euros – even at 1.4 to the pound that’s over £232. I
sourced a
suitable new ammeter from Richfield-Speedograph, got Bob Derrick of
Classic
Transfers to produce some small Indian script transfers, one of which I
applied
to the face of the ammeter. Next job was to make the box itself which
should be
aluminium, but I made mine in steel as it was easier to fabricate with
brazing.
The box was then painted silver to represent alloy.
I mutilated a new
Miller
headlamp switch that I had and set it in a piece of tufnol that screwed
to the
back of the box – job done – and all it cost was £18 for the ammeter
and £5 for
the transfers. Very satisfying indeed.
The
dynamo was already fitted but I had to get a belt and a pulley to
make it
run. The belt cost just over £2.50 off the Internet and the pulley I
obtained
from Alan Forbes the Indian Guru in Scotland.
At the same time as
ordering the pulley I also ordered a saddle pan as I needed to fit a
pillion
for my girl to ride on. The seats went to Dave Dalton, Mr Natural, for
recovering and after six months he did produce a good job. So I had the
pan
saddle – all I now needed was a pile of flat bar to make a replica
Meisinger
pillion seat frame.
I
was lucky enough to have taken a pile of photos
of an
original one in a museum in Holland
and emailed the curator who, very promptly, provided me with the cross
section
of each piece. Believe it or not but there’s three different sizes of
bar involved.
The seat was made and pan fitted – and so far Jean hasn’t fallen off
the bike.
The
bike came with a battery, but it wouldn’t fit in the battery box and
was
installed in the toolbox – problem was that I couldn’t get the top off
the
‘proper’ battery box without unbolting the whole lot from the frame -
well, I
wanted somewhere to put a few spanners etc. So, it was a case of
repositioning,
not by much, the whole tool and battery box assembly. That done and I
could
then get into the battery box. The battery seemed to be new and carried
a charge
ok; the only problem was that the first run must have shaken its inside
to bits
as it just wouldn’t charge afterwards. So I now have a gel battery
installed in
the correct battery box and carry the tools in the tool box – easy,
isn’t it.
Another
small job was on the right hand footboard – it looked as if a 30 stone
guy had
trod on it as it didn’t sit straight any more. I removed it and added a
couple
of blobs of weld to get the board to sit in the horizontal position.
Next
thing was a horn. You know, one of those things that you have to have
for an
MOT but never ever use. The Indian should have an electric one – pretty
unobtainable I reckoned, unless I buy one from Holland at a
cost of £125, plus a button at
£20. Not wishing to give the Dutch any more of my money, I ordered a
button
from our local Classic Bike Dealer, but gave up waiting for that after
a year,
despite several reminders and no apologies. What I did have, on the
shelf so to
speak, was a hand operated Klaxon and on inspection I found that the
maker’s
plate came from New York.
Ideal – so, a quick strip down, grease, adjust and repaint and my
problem was
sorted. Not a proper electric horn but a period one that would do.
Things
were now looking good and I was just about ready for an MOT, however
when
running the engine I had quite a bit of oil being pumped out of the
timing
chest mag drive hole. Maybe the oil seal was no good or missing I
thought as I
stripped the timing chest out. To cut a long story short I found out
that there
should have been a breather valve in the bottom of the timing chest
and, guess
what, it was missing. The photo shows the outline of where the valve
should be and it seems to be a square flat disc valve of sorts with
four breather slots.
Basically
it screws to the crankcase with two small screws and allows
the
crankcase to breathe, so without one, the motor, when the pistons were
on the
down-stroke just pumped oil into the timing chest and it had to come
out somewhere.
That was what was pushing oil out of the mag drive hole. Now, where do
I get a
crankcase breather valve for a 1925 Indian – if I just knew what it
looked like
I could make one? I was in contact with Steve Slocombe who runs the
AMCA
European Chapter and as I’d joined the AMCA sent him a note. Steve is a
Harley
specialist but as it happened he put me on to Robin Oakley in Kent
who
specialised in Indians. “I’ll have a look through my old stock for you”
he
said. Two days later I was able to uncross my fingers when Robin rang
to say
that one was on its way and could I send him a tenner. The item
consisted of a
disc valve, held in place by two small screws – fitted – and I had no
more oil
pumping out of the mag drive hole.
Please,
dear reader, don’t think that we’ve finished just yet. My next problem
was when
I found that when running the motor it would stop after a while. The
petrol tap
is one of the types that consists of a rod that screws down through the
tank in
order to cut the fuel off. What was happening was that the thread in
the bottom
of the tank was worn out and as soon as the tap was unscrewed the
vibration of
the engine just shook it back down into its seat, thus cutting off the
petrol.
There was only one thing for it I had to make a new threaded seat and
solder it
into the tank. So, out came the tank and I drained it of oil and petrol
as best
I could. Next came the job of purging the tank of petrol fumes so that
I could
use a naked flame on the bottom to get the old fuel tap seat out. I did
that as
I have always done – easy really – remove the tank filler cap, open the
petrol
tap in the bottom of the tank and turn it upside down. Pass a naked
flame over
the petrol tap and you’ll get a big bang as the fumes inside ignite and
blast
downwards out of the largest hole – the tank filler one. I’ve had tanks
lift 12
inches up off the bench when doing this. Afterwards a naked flame can
be used
on the tank quite safely. Out came the tap from the bottom of the tank
– gee –
what a shambles. Whoever had made it had no idea of how it should work
and I’m certain
that it wasn’t original. I turned up a new one in the form of a top
hat,
threaded it and soldered it back into the tank. As you might guess, it
ruined
the paintwork, but at least it was on the underside of the tank so
wouldn’t be
noticed, plus the tap worked correctly for the first time.
One
thing that I found was that when running the motor, it was getting far
too much
oil from the oil pump. The bike has a total loss oiling system so the
pump has
to deliver just the right amount and too much was going through. I
adjusted the
pump down as far as it would go to try and reduce the oil supply, all
to no
avail. Anyway, time was marching on and I, with loads of confidence,
had
entered the bike in the Saundersfoot run for 2008. After all, I’d had
it for a
year and hadn’t had a ride yet.
Next
job was an MOT – no problem at all. We did have a laugh over the lights
though
and as the tester set up his board at the end of the workshops about 15
feet
away, he asked me to turn the lights on. My comment was “don’t be daft;
the
light won’t get that far”. I was right and we had to turn the whole
workshop
lights off to be able to see the glow. Luckily, there is no
specification for
the brightness of a headlight, just a requirement for it not to dazzle
any
on-coming vehicle. I had my MOT, hooray.
Armed
with my new MOT, insurance certificate and dating certificate I set off
for the
DVLA office in Llanishen only to be seen by a young ‘jobs worth’. “Have
you got
the bike with you?” he asked, “No”, I replied. “Oh, but I have to see
it” he
said. I remonstrated with him that that had not been the case in the
past when
applying for an age related number. “It’s always been the case” said
jobs worth.
So, off I set on a 30 mile round trip to collect the bike and trailer.
Arriving
back at the DVLA offices I was served by an older guy with a beard. He,
checked
all my paperwork and said ”That’s
fine,
I’ll allocate a number”. “Don’t you want to see the bike?” I asked, as
politely
as I could. “No need for that” he said. OOOh, that was the wrong thing
for him
to say to me and I retorted “Oh yes, you will inspect it, as that lad
over
there has just sent me on a 30 mile round trip to get it”. Reluctantly
he
inspected the bike and allocated me a reg number and issued an amended
MOT
certificate. At last I could take the bike for a ride.
Number
plate fitted and the following day I was ready – gosh, there’s
something quite
exhilarating about the first ride on a new bike. The foot clutch was
something
new for me as I wobbled off down the road. Anyway, so far so good and
on each
ride I went a bit further afield. I soon found out that I had a problem
– right
foot needed for the only brake, left foot needed for the clutch, how
the hell
was I expected to take off on a hill!! I need another leg.
September
soon arrived and we were entered on the 1908 Triumph outfit to ride in
the Isle
of Wight September Scurry. I decided to take the Indian and then during
one of
the evenings could have some more short rides on it so that I could
become more
familiar with how it went. On the Island
it
soon became obvious that the single speed Triumph just couldn’t cope
with the
terrain so the Indian was pressed into service. I decided that the best
thing
to do with the oiling was to run the bike and not use the mechanical
oil pump.
Instead I’d rely on the good old fashioned hand pump giving a shot
every five
miles or so. That’s how we ran and as it happened the bike got along
very
nicely – at last I was enjoying it. It would woof up all the hills in
top gear
even though there seemed to be a need to rev the motor quite highly in
order to
get along at a decent speed on the flat. The following weekend we had
the
Saundersfoot run and I was now confident that we could ride that ok,
despite
the mechanical oil pump delivering too much oil. I had two days before
we set
off for the Saundersfoot event and decided to have a good look at the
oil pump
as it should work ok. I completely stripped the pump on the bench and
found a
small non return valve on the outlet. I could blow and suck through it
–
‘that’s not right’ I thought. I stripped the ball valve assembly and
found all
ok, then as I re-assembled it I found that the seat for the ball was
just not
screwed home properly. Job done – with any luck it would now work
properly.
Saundersfoot arrived and we set off on the 80 mile run – relying on the
mechanical oil pump to do its job – fingers crossed and all. Would you
believe
it – the pump worked as it should even though it provided just a touch
too much
oil. That was easily adjusted afterwards.
One
thing that I found was that my left leg muscles were giving me hell
after the
ride. The foot clutch was causing the problems, but it soon became
clear as to
why – I had been wearing my usual motorcycle boots and the ankles are
just not
designed to be flexible.
During
the winter 2008/09 I decided to have another go at curing the oil
seepage that
was coming from the head gaskets on both cylinders. In removing the
heads the
gaskets decided that they had had enough and decided to delaminate. Not
a
problem, I thought and I soon had some new gaskets made from some Lion
Brand
jointing that I had. All seemed ok now.
Next
outing was in May at the South West Coast Run near Bristol
and, despite the rain, we set off on the
run, full of confidence. Five miles or so down the road the front head
gasket
decided to blow a chunk out – that was quickly followed by a piece of
the rear
head gasket. Not a good day and there was no backup to rescue us, but I
did get
a lift back to the start and soon recovered the bike.
Back
at home I decided that copper head gaskets would be the answer, so cut
two out
of some copper plate. They needed quite a bit of heat to anneal them
but I did
manage it and they were soon fitted and the heads tightened down.
However there
was still some seepage of oil, which is more annoying than anything
else. Son,
Richard, who works for Honda came to the rescue and he gave me a tube
of grey
paste – “Try this stuff dad, Honda don’t use gaskets on their engines
any more,
just this paste”. Gee what magic stuff it is, just a smear on each side
of the
copper head gaskets and the problem has gone. The next weekend we
completed the
Seaside Run with no problems apart from finishing with a rather oily
engine,
but at least it wasn’t coming from the heads any more.
The
next event for the Indian was the Banbury run – we were to ride the B
route of
55 miles which included Sunrising hill. For some reason or other I had
entered
at a speed of 20mph instead of the optional 24mph, which would have
been
better. The bike managed the route with no problems and probably would
have
climbed Sunrising in top if it were not for the fact that the hill had
a large
number of spectators watching the bikes. I changed into second and the
bike just
romped up the hill with Jean and I on board. Back at the finish and I
parked
the bike and went off to see Terry and Dilys. An hour or so later we
returned
to the bike to find that there was not a drip of oil under it – no
leaks,
hooray. But I thought about it, surely the reason that the bike had not
leaked
was that we were not running the engine at high revs – a light lit up
in my
brain, it does sometimes!! What if the bike has sidecar gear ratios -
that
would make sense, as I have found that I don’t need bottom gear and
that the
bike takes off easily in second.
Back
at home I got my 1925 Indian handbook out and checked out the gear
ratios. As
the motor has a gear primary drive, ratios are altered by changing the
gearbox
sprocket. 20 teeth for solo, 18 teeth for sidecar and 17 teeth for
heavy
sidecar. Now to check what I have on the bike. The sprocket is hidden
inside
the chainguard and is difficult to see, anyway, a chalk mark on one of
the teeth
was all that was needed as I counted the teeth and turned the back
wheel. Would
you believe, not 20 teeth, or 18 or even 17 – I had a 14 tooth
sprocket. Just
wish that I knew the Dutchman who’d built the bike as I could post him
the 14t sprocket
to shove where the monkey puts his nuts. I got onto Robin Oakley again
and
after a chat we decided that an 18 tooth sprocket would be best, as it
would
make the bike more ‘user friendly’ in the UK.
We just don’t have the long straight
roads of the USA,
so the need for ‘long legs’ just isn’t there. Robin supplied me with a
nice new
sprocket and luckily the chain still went on with the rear wheel in its
foremost position.
Is
that it? Do I now have a usable Indian? Not quite as I found that the
front two
tank mounting bolts had decided to spring leaks. One under the oil tank
and the
other under the petrol part of the tank. Off came the tank again and I
soon re-soldered
the fittings, only to find that the petrol one did not seal properly.
The
fittings were small top hat types that were just soft soldered into the
bottom
of the tank. Obviously different to the proper fittings at the rear of
the tank
– no doubt, another Dutch bodge. I turned up some new brass fittings
with a
much bigger area for soldering and they were soon fitted. Watch this
space as the
saying goes, but so far all road tests have shown no further problems
and what
a nice bike it is to ride.
Progress
on the speedo setup is coming along well. I was lucky to find a Corbin
body in my garage. The drive ring came from Ebay, the gearbox is a
British one and will do for now, whilst the stainless drive cable is
from a shower unit and cost £1,99. I had to use Photoshop to produce a
face for the head and also had to make a needle. I fully expect it to
be totally inaccurate when it's fitted, but it will look good.
August
2009
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